Beckhoff · AX5000 Servo Drive
This error indicates that the motor's commutation results are incorrect, meaning there is a misalignment between the motor's electrical phases and its physical rotor position. This can occur during initial setup, especially with "wake & shake" procedures, or after motor/encoder replacement. Incorrect commutation leads to inefficient motor operation, poor control, and a significant risk of uncontrolled movements or damage, compromising safety and performance.
Click steps to track your progress.
Verify motor phase wiring (U, V, W) matches the drive's output terminals (T1, T2, T3) according to the motor manufacturer's specifications.
Inspect the motor encoder cable for damage and ensure it is securely connected to the drive's feedback input (e.g., X10). Measure encoder supply voltage (e.g., 5VDC) at the motor connector.
Execute the automatic motor identification or commutation alignment routine provided by the drive (e.g., setting P-0-0006 to 1 and initiating).
Check for mechanical binding or obstruction on the motor shaft that could prevent smooth rotation during commutation.
If using hall sensors, measure the output voltage of each sensor (e.g., 0V or 5V) while slowly rotating the motor by hand.