SEW Eurodrive · MOVIDRIVE system
The motor current flowing through the output stage is excessively high, potentially due to an undersized motor, issues with the current supply or transformer, incorrect ramp times, a defective phase module, or an unstable 24 V supply. This condition can lead to severe damage to both the drive and the motor if not corrected.
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Monitor the actual motor current (e.g., Parameter P7-01) during operation and compare to the drive's rated output current and motor nameplate current.
Increase acceleration time (e.g., Parameter P3-04) and deceleration time (e.g., Parameter P3-05) to reduce current peaks during speed changes.
Measure the mechanical torque required by the load using a torque wrench or appropriate sensor to verify it's within motor specifications.
Verify motor parameters P3-01 (Rated current), P3-02 (Rated voltage), and P3-03 (Rated frequency) are correctly entered into the drive.
Disconnect the motor from the mechanical load and run the drive in no-load condition to isolate if the fault is mechanical or electrical.