Lenze EVF9300 Vector Drive

60 fault codes documented

011

OC1

A short circuit has occurred in the motor cable, or there is excessive capacitive charging current if the motor cable is too long or has high capacitance. This can lead to drive tripping and potential damage.

012

OC2

One of the motor phases has made contact with earth (ground), indicating an earth fault. This suggests an insulation breakdown in the motor cable or the motor windings.

015

OC5

The drive is experiencing an I x t overload, characterized by frequent and excessively long acceleration phases with overcurrent, or continuous overload where Imotor > 1.05 x Irx. This indicates that the drive is undersized for the application.

016

OC6

The drive is experiencing an I²xt overload, characterized by frequent and excessively long acceleration processes with motor overcurrent, or permanent motor overload where Imotor > Irmotor. This signals a prolonged motor overload condition.

018

I²xt overload advance warning

This is an advance warning for an I²xt overload, indicating frequent and excessively long acceleration processes with motor overcurrent, or permanent motor overload where Imotor > Irmotor. It signals an impending trip condition if conditions do not change.

0209

float Sys-T

A float error, such as division by zero, has occurred in the system task (ID 0) during real number calculations. This indicates an issue within the program code's arithmetic operations, leading to an imprecise or undefined result.

0210

float Cycl.-T

A float error, such as division by zero, has occurred in the cyclic task (PLC_PRG ID 1) during real number calculations. This indicates an issue within the PLC program's arithmetic operations that impacts the cyclic execution.

0211

float Task1

A float error, such as division by zero, has occurred in task 1 (ID 2) during real number calculations. This indicates an issue within the program code specific to task 1's arithmetic operations.

0218

float Task8

A float error, such as division by zero, has occurred in task 8 (ID 9) during real number calculations. This indicates an issue within the program code specific to task 8's arithmetic operations.

0219

overrun Cyc.-T

The cyclic task (PLC_PRG ID 1) has exceeded its allocated monitoring time. This indicates that the task processing duration is longer than the set monitoring time, potentially due to complex or lengthy program parts.

0220

noT-Fkt Credit

The controller lacks the necessary technology units to execute a loaded program containing technology functions. This indicates a mismatch between the program's requirements and the controller's hardware capabilities.

0230

No Program

No PLC program has been loaded into the controller's memory. The controller is unable to execute any programmed logic or control functions without a loaded program.

0231

Unallowed Lib

The PLC program attempted to call a library function that is not supported by the current controller hardware or firmware. This means a required hardware component might be missing, or the function is incompatible with the controller variant.

0232

NoCam Data

Motion profiles (CAM data) are not available in the controller's memory, despite functions from the `LenzeCamControl.lib` library being called. This prevents motion control functions from operating correctly, potentially due to incorrect project setup or a reset.

032

LP1

A current-carrying motor phase has failed, or the current limit value is set too low. This can lead to irregular motor operation, reduced performance, or motor damage.

050

OH

The heatsink temperature has exceeded +90°C. This is often caused by an ambient temperature greater than +40°C or +50°C, a dirty heatsink, or an incorrect mounting position, leading to potential overheating.

065

CE4

The controller has entered a BUS-OFF state on the system bus (CAN) due to receiving too many faulty telegrams, leading to disconnection from the bus. This indicates a severe communication breakdown.

066

CE5

A time-out has occurred on the system bus (CAN) during remote parameterization (C0370, C0371), indicating a communication error of the gateway function. The slave device did not respond within the communication monitoring time.

070

U15

The internal 15V voltage supply is experiencing an undervoltage condition. This affects the internal control electronics and can prevent proper device operation.

071

CCr

A system failure has occurred due to strong interference injection on the control cables. This can be caused by inadequate shielding or ground/earth loops in the wiring, leading to unstable operation.

072

PR1

A checksum error was detected in parameter set 1 during loading or transfer via the keypad. This indicates a fault in the parameter data or incompatibility with the loaded software version. The Lenze default settings are loaded automatically.

073

PR2

A checksum error was detected in parameter set 2 during loading or transfer via the keypad. This indicates a fault in the parameter data or incompatibility with the loaded software version. The Lenze default settings are loaded automatically.

074

PEr

An error has occurred in the program flow, indicating an internal software issue within the device. This may lead to unexpected behavior or system stoppage.

075

PR0

An error exists in the parameter set, often triggered after an operating system software update. The device automatically loads the Lenze default settings.

077

PR3

A checksum error was detected in parameter set 3 during loading or transfer via the keypad. This indicates a fault in the parameter data or incompatibility with the loaded software version. The Lenze default settings are loaded automatically.

078

PR4

A checksum error was detected in parameter set 4 during loading or transfer via the keypad. This indicates a fault in the parameter data or incompatibility with the loaded software version. The Lenze default settings are loaded automatically.

079

PI

A fault occurred during parameter initialization, likely during parameter set transfer between two devices, or because the parameter set does not match the controller (e.g., from a higher-power controller to a lower-power one).

080

PR6

The device has reached the maximum allowed number of user codes. This prevents the creation or storage of additional user-defined settings.

082

Sd2

A resolver error has occurred at terminal X7, typically indicating an interrupted resolver cable. This prevents accurate position feedback.

083

Sd3

An encoder error has occurred at terminal X9, typically due to an interrupted encoder cable or pin X9/8 not being connected. This can lead to incorrect or no position feedback.

085

Sd5

An encoder error has occurred at X6/1 and X6/2 (when C0034 = 1), indicated by a current signal less than 2mA at these terminals. This suggests an open circuit or a faulty current signal encoder.

086

Sd6

The encoder for detecting motor temperature at X7 or X8 is indicating undefined values. This suggests a problem with the temperature sensor, its cable, or connection.

087

Sd7

An initialization error occurred at the absolute value encoder at X8, or the encoder electronics are defective. This can result from a loose cable, an open circuit, an incorrect encoder type, or failure during rotor position adjustment.

088

SinCos encoder at X8 sends inconsistent data.

The SinCos encoder at X8 is sending inconsistent data, indicating damaged internal tracks or high interference on the encoder cable. It could also mean the encoder is not transmitting data due to an open circuit, an incorrect encoder type, or a defective sensor.

089

PL

The rotor position adjustment was canceled, possibly due to an Sd7 or Sd8 error occurring during the adjustment with an absolute value encoder. This error is saved with mains failure protection.

091

EEr

External monitoring has been triggered via the DCTRL input. A digital signal assigned to the TRIP-SET function has been activated.

1020

OU

An overvoltage condition exists in the DC bus, where the DC bus voltage is higher than the value set in parameter C0173. This is typically caused by excessive braking energy being fed back to the bus.

1030

LU

An undervoltage condition exists in the DC bus, where the DC bus voltage is lower than the value specified in parameter C0173. This typically indicates insufficient input power to the drive.

105

H05

An internal fault related to the device's memory has occurred. This typically indicates a hardware issue that requires specialized attention.

107

H07

An internal fault related to the power stage has occurred. During the initialisation of the controller, an incorrect power stage was detected, indicating a serious internal hardware issue.

110

H10

The sensor for detecting the heatsink temperature is indicating undefined values. This suggests a fault with the sensor or its connection, leading to unreliable temperature monitoring.

111

H11

The temperature sensor inside the controller is indicating undefined values. This suggests a fault with the sensor or its connection, leading to unreliable internal temperature monitoring.

151

Error "negative limit switch".

The negative limit switch has been reached, preventing further movement of the drive in the negative direction. This is a safety mechanism to prevent overtravel.

152

Error "positive limit switch".

The positive limit switch has been reached, preventing further movement of the drive in the positive direction. This is a safety mechanism to prevent overtravel.

153

Following error

The angle difference between the set position and the actual position is larger than the following error limit set under parameter C0255. This can also indicate the drive cannot follow the digital frequency due to reaching its Imax limit, suggesting insufficient drive dimensioning.

154

Error "negative position limit".

The negative position limit (C1224) was not reached, potentially due to incorrect position targets or issues with the 'set function position value'. This can prevent the drive from reaching its intended negative travel extreme.

155

Error "positive position limit".

The positive position limit (C1223) was exceeded, potentially due to incorrect position targets or issues with the 'set function position value'. This can cause the drive to overtravel its intended positive extreme.

156

No reference.

The reference point for the drive is not known. In absolute positioning mode, homing was not performed before the first positioning command, which is essential for establishing a known position.

157

Parameter set mode is absolute instead of relative.

An absolute parameter set (C1311) was performed or is active during relative positioning (position mode C1210). This mismatch in positioning modes prevents correct operation.

158

Error "actual reference dimension offset".

The actual reference dimension offset (C1226) is outside the defined position limits. This indicates an error with the program function 'set position value' or incorrect limit settings.

159

Error in positioning program.

The positioning program contains impermissible programming. Specifically, a parameter set with a final speed must be followed by a parameter set with positioning, and it is not permissible to wait for input at that stage.

162

Error in the range of the encoder.

The traversing range of the absolute encoder has been exceeded. This means the physical travel of the drive has gone beyond the measurement capabilities of the installed encoder.

252

AddData DlErr Error during FLASH memory access

An error occurred when downloading data into the FLASH memory. This can be caused by a time-out, transmission error, or a mains failure during the data transfer process, resulting in incomplete or corrupt data.

260

Err Node Guard "Life guarding event"

The controller, configured as a CAN slave, did not receive a 'Node Guarding' telegram from the CAN master within the configured 'Node Life Time'. This indicates a loss of communication supervision on the CAN bus.

x220

CDA

An attempt was made to transmit profile data that was detected as faulty. This typically occurs during communication processes involving profile data transfer, indicating data integrity issues.

x221

CDA-LOAD

A checksum error was detected for the transferred profile data, indicating corruption or an incomplete transfer. This means the integrity of the loaded profile data is compromised and may lead to incorrect operation.

x240

ovrTrans Queue

The transmit request memory has overflowed, indicating too many CAN objects are queued for transmission. This can lead to delays or loss of communication on the system bus.

x241

ovr Receive

Too many receive telegrams are present on the system bus (CAN). This overload can cause issues with processing incoming communication data, potentially leading to lost messages or communication delays.

x250

2.Flash Err

An error occurred during access to the FLASH memory, indicating the PLC program attempted to access non-available or defective memory. This could signify a hardware issue with the FLASH memory module, preventing proper program execution or data storage.

x251

AddData CsErr

A checksum error occurred when loading data into the FLASH memory. This indicates data corruption during the transfer process to non-volatile memory, which can lead to incorrect program behavior or lost settings.